PFC Part 3: The controller

All this power is nothing without control.

Luckily by using silicon carbide power devices, we were able to handle all the power we needed with a simple boost converter switching at 100kHz. No need for multi-phase or fancy energy recovery snubbers- it’s just a domestic appliance-sized PFC front end scaled up.

This means we can also use a controller intended for said domestic appliance PFC. I used the UCC28180 PFC controller chip from TI, because it only has 8 pins and is marketed as “easy to use”, therefore it can’t possibly go wrong! πŸ˜€

(OK, I bought the evaluation board and tested it with some Tesla coil-like loads before committing)

The PFC controller as built

This is the circuit I ended up using. It’s quite different to the original TI application circuit, so I’ll describe the differences.

Compensation: TI provide 2 full pages of formulae for calculating the compensation components, and ain’t nobody got time for that! So I took the values from the evaluation circuit, and doubled the capacitors and halved the resistor because it seemed like a good idea.

Gate drive: Silicon carbide MOSFETs need a negative gate voltage to turn off, and the UCC28180 doesn’t provide this, so I had to make a separate gate driver, which I’ll describe in the next post. The Silabs isolated gate driver chip needed a 5V supply and a 5V signal, so I had to add a level shifter and a 5V regulator.

Inductor current feedback: The UCC28180 is designed to take feedback from a resistor in the DC bus negative. This is a very common design choice in small PFCs. I added the 4x 1N5819 diodes and associated circuitry to adapt the signal from the CTs to look like it came from the original resistor. The 13V zener is used to clamp the spikes when the CT cores reset. A value of 13V guarantees reset even with the maximum duty cycle allowed by the controller chip.

I tested the CT feedback on the UCC28180 eval board before committing to building the full sized version, in case the chip turned out to be unhappy with it for some unforeseen reason, but it performed identically to the original resistor feedback, as far as I could tell.

Voltage feedback: Since the CTs provide isolation of the current signal, and I ended up using an isolated gate driver, I decided to isolate the voltage feedback too so the control circuit would be completely isolated from the high voltage side. I used a simple circuit based on the HCNR201 linear optocoupler and a TL071 opamp.

Voltage feedback isolation circuit

The voltage feedback input of the UCC28180 has a high enough impedance that it can accept the current from the photodiode (4.5uA per 100V DC bus voltage) directly with no amplification or buffering. This simplifies the circuit considerably and provides some nice synergy. The UCC28180 has circuitry to detect an open feedback network, a dangerous condition that can cause the output voltage to run away, blowing up expensive pieces of power electronics. By configuring the voltage feedback in this way, the protection still works for an open circuit anywhere in the signal path, including forgetting to plug the isolator into the main board, and loss of power to the isolator’s opamp.

The controller. Knob is for output voltage adjustment.
The voltage feedback isolator

Both circuits were easily constructed on protoboard with through hole components (and an adaptor for the UCC28180)

PFC Part 2: The engine

When I started designing I already knew that the heart of the thing would be silicon carbide MOSFETs and diodes. I heard so much from Anders Mikkelsen of Advantics raving about how awesome they are. πŸ™‚

On recommendation from Anders I chose the C3M0065100K MOSFET and C4D10120D diode. These are available from Farnell, Mouser etc. for about Β£10 each. I figured that 2 in parallel would allow me to run an inductor current of 32A RMS, a reasonable match to the mains supplies available in the UK and Europe. Anders also kindly donated an inductor capable of handling 32A RMS. πŸ™‚

The remaining design decisions were set by the dumpster find of a large heatsink and set of 3 Semikron dual diode bricks. Having such a beefy oversized rectifier made short circuit protection easy: I just needed to come up with one more heavy duty diode to bypass the delicate SiC diodes, and then a short on the output would simply pop the circuit breakers on the mains input.

Schematic of the boost PFC engine

CT1 and CT2 are small ferrite cored 1:200 current transformers sensing the MOSFET and diode currents. Their outputs are combined in the controller to give the inductor current.

DIY 3 layer PCB πŸ™‚

SiC MOSFETs can switch incredibly fast, so a good layout with minimal stray inductance is important. I decided to make a multi-layer structure out of pieces of single-sided copper-clad PCB and copper sheet.

Trial fitment of the components.

I didn’t manage to fit as many capacitors as I wanted: only 5 on the input and 4 on the output. The output ones in particular will have a hard time with serious amounts of HF ripple current. They are only there to filter out the HF ripple. Large electrolytic capacitors will be needed to handle the power frequency ripple, they will be mounted somewhere else and connected by wires.

Assembled

Clamps for the MOSFETs and diodes made from pieces of Ikea cabinet legs. πŸ™‚

PFC Part 1: Background

I decided it was time to build a new power supply for Odin with power factor correction. (See all posts on the PFC)

Power factor what? To explain, we have to go back to the turn of the last century and the War of the Currents. Alternating current won so all of our mains supplies are AC. However, solid-state Tesla coils, like most power electronics, run off DC. Odin needs several kilowatts of power at about 750V DC.

The simplest way to achieve this is to use a voltage doubling rectifier on the 240V AC mains. I used this in my previous large solid-state Tesla coil, the OLTC2, with one small refinement. I used SCRs instead of diodes to allow soft starting and varying the output voltage.

The major drawback of this circuit is a very poor power factor, especially at reduced output voltage. It is particularly bad in a DRSSTC, as it has a huge capacitor on the DC bus for energy storage, and the rectifier charges this directly. I improved the power factor somewhat by connecting a large iron cored inductor in series with the incoming mains. This worked well enough, and you can see details of the old power supply here here and here.

Gate pulses, line voltage and line current waveforms from the old PSU running at low output voltage.

I used this same power supply topology in Mjollnir, Little Cook and Odin. There was no room inside the smaller coils for the passive PFC inductor, so I used a much smaller one, making the power factor even worse. The shortcomings really became apparent in a few shows I did with Odin. It performed really badly when running off a generator, and there were two venues with 3 phase supply that I couldn’t use.

After much thought I decided to go for the simplest possible solution: a boost PFC. These are very common in larger consumer electronics, and controller ICs and design information are readily available. It is also easy to modify for 3 phase input. Essentially you just replace the rectifier with a 3 phase one. The line currents aren’t nice sine waves any more, but the power factor is still greatly improved over a plain rectifier with the same filter capacitance.

Probably the biggest drawback for Tesla coil use is that the output voltage can only be greater than the peak value of the rectified input voltage. You are limited to a minimum of about 400V when running off 240V single phase, and 600V from a 415V 3 phase supply. This is a problem for me at least because I like to check the tuning at reduced voltage after setting the coil up at a new venue.

Eventually I persuaded myself that I could live with this and set to work designing a boost PFC.